Thanks for the kind words and suggestions guys!
Well what a day it has been! It's taken me 12 hours however I can say that the car is now sorted and moving under its own steam again
Having spent the morning toying with he running issues at hand and bouncing ideas off a few people (Mainly Ali who has been my Yoda for the last two days and listening to all of my wims and questions, even taking time out of his working day to call me to talk things over), it was eventually concluded that it must be an exhaust leak that was causing all of the issues... The exhaust colour in particular supported this!
All of the ingredients were otherwise there... (Thank you to those who suggested this). Fuel, air and ignition were't issues so it meant I needed a new exhaust gasket at 10.30am
with nothing off the shelf in the UK in lots of cases.... Call in Mike from MJP (Hero of the Day) who had stock, realising my need and that my second day off was wasting away, a three hour round trip to Essex with the Dartford crossing done twice and I was back home with a new exhaust manifold gasket. Thank you Mike, really appreciated the assistance! (Perhaps on reflection should have tried the nearer venue in Fourways!
)
Much to my joy I stripped everything back down again (much faster this time having done it before). Other than getting a ratchet spanner stuck on the header for a time this actually went quite smoothly. Got the old gasket off and cleaned all of the surfaces again thoroughly before dropping the new gasket in place. Not taking any chances I also smeared the back of the intake manifold ports with Loctite high temp gasket to make sure it really sealed.
Back to putting everything back into place again and tightening up so that we were all good, I made sure to replace some of the copper exhaust manifold nuts with spreader plates and smaller nuts to really make sure everything was secured this time as well. Key in the ignition and moment of truth time, full choke and she fired right up, shooting to high rpm.... Choke backed off and she was idling like a dream, queue me running around my driveway with my arms in the air like a footballer celebrating...
Carbs balanced and running well, so all fears confirmed and resolved. Heat shield reinstalled and ITB socks installed to get the car running on the road again.
Next up was the dreaded steering coupler, taking no chances I called in the big guns and got some 300mm pliers from B&Q which gave me exactly the leverage I needed to squeeze the poly and pop the bolt back in like a dream, steering is only every so slightly off but very much reconnected. Some stainless steel cable ties to help with my exhaust hang while I sort out a more permanent central bracket and it was time for a test drive....
All I can say is wow, I let the car get up to temperate first but could tell that the car felt keen from the get go. It has a great burble at low rpm without being too intrusive. Once up to temp and with the loud pedal pushed and it just goes.... Pulls strongly to around 5k rpm however the magic really starts at 4k rpm where it just sounds asbo loud and bonkers and starts screaming! and then when you lift off it just pops and crackles and farts like a symphony orchestra. Amazingly at motorway speeds though its very refined (unlike the ind noise and rattles) Safe to say I spent 30 minutes grinning like an idiot blasting around the local roads, most definitely holding onto gears longer than Miss Daisy would have approved of just to keep ringing it out. Really quite impressed with the difference its made, certainly no restrictions in the exhaust now.
At this point I really do need to give a shout out to everyone who has had input, there's been some superb advice and encouragement from the community. This is certainly the most challenging job I've completed on the car however it wouldn't have been possible without all of the help of lots of people, so thank you! I owe several people beers now...
The car is out tomorrow to be dropped off to friends at a local restoration company, the handbrake cable needs changing and I've had enough of crawling around on the ground even if I could sort it. Their high lift will make short work with the great access... Ordered one replacement from Thailand for a great price and to my surprise had two turn up on different days so that was a bonus to now have a spare...
Lots still to do, I'm hoping to get an airbox setup sorted out soon enough all being well, strut braces need to make their way back from San Fransisco and I'm getting desperate to upgrade the front brakes in some way however I've rambled on too long as it is already, here's some pictures from my very long day which for the second time in a row ended up finishing in the dark!
So here was out big give-away as to where the problems were, no real heat going through the left bank....
IMG_9393 by
Mark Woodrow, on Flickr
Messy....
IMG_9403 by
Mark Woodrow, on Flickr
Clean
IMG_9419 by
Mark Woodrow, on Flickr
Fresh!
IMG_9420 by
Mark Woodrow, on Flickr
Reassembly
IMG_9424 by
Mark Woodrow, on Flickr
Not taking any chances... Hard to clean a load off as I realised I'd gone a bit mad and didn't want nay finding its way into the intake!
IMG_9429 by
Mark Woodrow, on Flickr
All good to go
IMG_9434 by
Mark Woodrow, on Flickr
Nice run underneath
IMG_9387 by
Mark Woodrow, on Flickr
The steering coupler fixer!
DA1D76DE-046A-4EAB-A14E-2B7EA6A0CF0C by
Mark Woodrow, on Flickr
The finished product! (more to come in daylight rather than floodlight)
IMG_9439 by
Mark Woodrow, on Flickr